Thanks John.
I was using garnet grit, not silica sand, but I still wear a twin-filter respirator mask when doing any grit-blasting. The grit I have been using is too expensive to consider for a larger scale setup. It is $36 for a 25kg bag, which doesn't go far, even with the little system I have with a 5 cu/ft a min compressor. We actually have a monster of a compressor that is no longer used at work, but it's 3 phase. Ideally, I would take the truck to work and blast it there, but the landlord, Council and a dozen or so neighbours in the middle of the city are sure to complain. If I pinched it, I suppose I could set it up to run off a petrol engine, but the actual compressor is not designed to run like that. It's setup to shut off the electric motor when pressure hits a set point and I really need one like in the trucks, that holds the valves open and allows the engine to continue running.
I did some checking with local grit blasters and they all use silica sand or steel shot for the really big jobs and they gave me their supplier's details. Unfortunately, being Xmas, they were shut early. All I got out of them was that they sell a few different sizes of grit, either in 20kg or 1.2t bags.

No prices until they are back on the 4th.
I did get a new toy though. Its a Skillmeister portable sandblaster. It has a tank that holds up to 40 litres of sand and is actually pressurised. It has a 10' hose and a selection of ceramic tips for different sizes of grit. I priced them locally and they were $297.99. I got mine for $70 and a 2hr round trip to collect it. It has only had 10kg of grit through it and there isn't a mark on it. I think it should be a big improvement over my current gear.
The transfer case is pretty much ready to repaint and refit, but I have to clean and paint the chassis rails and a lot of other things first. Today I got started on that. I already took the driver's side fuel tank off a while back and today I took the other side off. Eventually. It seems that over winter/spring, all my tools migrated from the truck back to the house and my car. Every time I went to do something, I found I needed something that wasn't there. The 2 straps that hold the tank on the support brackets were almost rusted through, so I cut through them with the grinder and took the tank off. The support brackets are still solid, but the shields are pretty much stuffed. I got 2 of the bolts out of the first bracket, but the other 2 were too rusted so I cut them off with the grinder and knocked them through with a punch. The 4 bolts on the rear tank support are behind the winch and it was too hard to get at them, so I cut the heads off with the grinder. See a pattern?

I tried to get the air actuator for the winch off, but the clevis pin is stuck in the fork on the end of the actuator arm and it's not positioned where I can tap it through with a punch. I gave it a good spray with CRC and will try to turn it with vice-grips tomorrow.
I finally got the last bolt out of the rear drive-shaft flange. Last summer, 3 came out easily but the nut on the fourth was very pitted and I couldn't get a socket or spanner to grip it. Today I jacked up a rear wheel and turned it until I could get at the nut better. After heating it up with a LPG torch, I tried again but the nut was too deformed to get a socket on, so I ran a thin cutting disc on the grinder through the side of the nut and split it with a cold chisel. Even then, I had to knock the bolts through with a punch as they were seized too. At least its done now and I have more room under there to work.
Whoever used the winch last wound it in so far that the eyelet on the end is tight up against the cable guides at the front. The cable doesn't have enough slack in it to lift out of the guides so I can run it out the back and then wind it onto the drum before dropping the winch out. I tried pulling it out using my car, but just dug holes in the ground. I had a look at the winch and the actuator shows the winch is in the "engaged" position. I tried to disengage it, but even with a 24" set of Stilsons on the actuator rod, it didn't budge an inch. I was worried about breaking something if I used more force so tried winding it out using the drive flange. After removing the short drive-shaft, I used a 3' length of flat steel across a couple of bolts through the flange, and there was no way it was going to work. The flange would turn about 25 to 30 degrees and stop. I suspect it is the slack in the worm drive. Either something is seized on the winch drum shaft or the brake band is locking on. Tomorrow I will pull the back off the brake box and pull it's guts out.
I took the drive flange off and gave it a clean and prime. The threads in the shear-pin hole were badly damaged when a previous owner sheared the pin, then welded it back together. He damaged the threads on the pin when grinding down the weld, which allowed the pin to move in the hole. I only had a straight sided bottoming tap, and it was a real bugger getting it started without it cutting a new thread, but I finally got it done. I tried it out with one of the new shear-pins I got from Mick_Marsh and it screwed down firmly with no movement. After I cleaned the drive-flange, I found it had a big letter "A" stamped on the edge, showing it had the EMEI mod done that called for it to be bored out slightly so that if the pin sheared and the winch drive-shaft kept spinning, that the flange wouldn't seize on the winch-box shaft.
Got the week off between Xmas and New Year, so I hope to get lots more done. Maybe some pics next post.
Greg.